March 18, 2009 8:34 PM Do you want to hear the motor?
Del Corey, Kathy, Scott Purcell, Scott's employee Jerry and I did the
first engine test today. THANK YOU GUYS. That is/was special to have the
necessary help.
NOW, do you want the good news or the bad news............. we did the
engine test today, over all it went pretty good except the guy who did the
sanding of the deck, installed the fuel pump, cut the threads of the water
in fittings and did the wiring, should update his resume.... ME!!!!!!!
Now to explain the above. I sanded for 17 hours and I thought the deck was
a flat as a bread board, after the clear was put down, it shows that it
isn't perfect. Then we first tested the water in to see if we
had any water leaks in the motor - it didn't but it did have two leaks
before the water even got into the engine. FIXED that, the put some fuel
in and found that the same above mentioned guy installed the fuel pump
backwards, FIXED that and then found a small fuel leak at the
carburetor - FIXED that.
Finally got to the point where we could fire the engine - except the same
above mentioned guy didn't wire the wire that goes between the distributor
and coil. FIXED that and it was time to LIGHT the candles up. It sounded
great....... STRONG. We ran the motor for around 5 minutes.
Did some minor adjustments and fired it up again for another 3 minutes,
but heard some in-correct noise. We decided to check the valves and jets
and spark plugs. We found we were running a little LEAN, so I changed the
jets up two sizes and we were adjusting the valves when Scott discovered a
problem with TWO rocker arms (the same guy that did all of the above
adjusted two rocker arms incorrectly (2 of 12) and it did some damage
to the end of the two rocker arms (I will need to install two new ones now
when I put the engine back together).
Everything has now STOPPED. I will now have to remove the two cylinder
heads, take them back to my machinist and have six of the 12 valves
replaced with longer valve stems (.020 longer). Then re-install the heads
and then Scott is coming over to the house to help me adjust the valves
correctly.
It is a minor setback and I should have the motor torn down by tomorrow
and get both heads up to the machinist for work. Scott says we will be at
Moses Lake heck or high water... We might be down for about a week or week
and a half. I still have to order new gaskets.
The attached pictures are from today and the YouTube video is from today
(Harold you mentioned you might put a 1981 picture out on the website,
beside a 2009 picture, will one of these work, or do you want the center
cowl on also).
If you want to watch the YouTube video it might take a little while to
load, but I think it is worth it. Turn the volume UP and the smoke you see
it the paint on the headers burning. I will making a change there also.
They will be going off to the powder coater and they will be ceramic
coated....
Oh, by the way, the bad noise you hear at the VERY end of the video is the
flywheel hitting the motor mount. We have now fixed that opportunity
also....
Pre-race bugs - one by one being worked out.
This actually is the first video (Kathy took about 9 video segments),
but we didn't run the engine very long, so Kathy took the first one I
sent you when we restarted the engine.
I like this on because at the first sign of FIRE, I gave Kathy a BIG
thumbs up.
BTW, the reason why the engine STOPPED so abruptly(and if you and read
body language, Scott Purcell and I are looking at each other to see
who did what - the owner forgot to turn on the electric fuel pump
switch (Scott, put that memory in your memory bank - flip up the fuel
pump switch to ON). So the engine will run exactly 47 seconds on the
fuel that is in the float bowls.... LOL
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